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  #1  
Unread 07-08-2011, 05:10 PM
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phatdaddy phatdaddy is offline
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Default outboard gods , need help

having a fuel problem, tell me what you guys think:

motor: 94 150 Merc 2.0
symptoms : bogs down on take off. intermitent might do it once out of 5 take offs

what i have done so far: changed fuel pump checked all fuel lines and tightened
checked filter

i concentrated on the fuel delivery because the ball would be empty. but the fp took care of that, now the ball remains hard. would a carb problem cause this symptom? the motor is 18 years old (1400 hrs)and i have never had the carbs off.
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  #2  
Unread 07-08-2011, 11:33 PM
Monkey Butler Monkey Butler is offline
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Carb cleaning would be my guess.
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  #3  
Unread 07-09-2011, 02:40 AM
Hedge Hedge is offline
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Sound to me like a float is sticking or possibly trash in the bowl.
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  #4  
Unread 07-09-2011, 01:23 PM
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It wouldn't hurt to clean the carbs, and make sure and put new kits in them when you do it. New carb kits should have viton needle and seat sets(grey tips) in them where as the older sets had neoprene needle and seats(orange or red tips). The viton holds up to ethanol much better than neoprene does.
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Unread 07-09-2011, 05:02 PM
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listen to what Ferm said
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  #6  
Unread 07-09-2011, 05:57 PM
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additional info, about 6 weeks ago, the tach started reading funny, but i would tap it and it would read normal. then it got where that would not work. if i turned it off and back on, it go to normal. i replaced the tach, no change. i swapped the tach lead on the voltage regulators, no change. charging voltage is fine 12.9 idle. & 14.1 running. anytime i have had a tach issue, stator is soon to follow, could this cause the bogging down?

i will do the carbs, with merc oem kits..
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Unread 07-09-2011, 07:14 PM
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Quote:
Originally Posted by phatdaddy View Post
additional info, about 6 weeks ago, the tach started reading funny, but i would tap it and it would read normal. then it got where that would not work. if i turned it off and back on, it go to normal. i replaced the tach, no change. i swapped the tach lead on the voltage regulators, no change. charging voltage is fine 12.9 idle. & 14.1 running. anytime i have had a tach issue, stator is soon to follow, could this cause the bogging down?

i will do the carbs, with merc oem kits..
Yes, a failing stator will cause all kinds of issues. MERCURY uses a 2 sided stator with a low side and a high side. It's right around 2500-3000 where the stator changes over I believe.
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664
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  #8  
Unread 07-25-2011, 09:45 AM
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I would bet on ther stator going bad
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