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			#1  
			
			
			
			
			
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|  1972 OMC 60HP Help 
			
			Hey guys I need some help.  I have a 1972 60hp OMC three cycle that surges like it not getting enough gas at high speed (4200 - and above) but the primer bulb is solid and squeezing backs no difference. Motor is making good power all along - just feels like it leans out at high speed. If you run it a lower speeds no problem. Here what I've done to the motor to date. Compression is 130 in all three holes. Rebuilt carbs Replace fuel pump/and gas lines New CDI amplifier New points New plugs Checked timing/TDC and there all good. One additional problem I noticed to day is at low speed the (1000 - 1200 rpm) the tach will occasionally spin the needle right around the dia making a 360 rotation before it settles back on correct RPM. Not sure if this some other problem or perhaps related to the issue I'm having at speed? Any suggestions/ideas.... | 
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			#2  
			
			
			
			
			
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			Are you sure you got the float levels set correctly? Sure sounds like one running out of fuel from your description. Or it could be a bad fuel pump dumping fuel into the engine.
		 
				__________________ 2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD  AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664 | 
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			#3  
			
			
			
			
			
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			Ferm Thinking about running with the air silencer off and using my hand to determine if its fuel related for sure by choking each carb individually and perhaps I'll be able to narrow down which one it having the issue at the same time. I'm pretty sure the float levels are good but I'll pull and verify. Not like I haven't had them off five or six times already. Kamikaze 
				__________________ 74 V20 CC with a 150 Johnson (Gone but not forgotten) 89 V20 Cutty with a Tower (Build in process) | 
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			#4  
			
			
			
			
			
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			anytime i had a wacky tach, stator gave trouble later on.
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			#5  
			
			
			
			
			
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				__________________ 2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD  AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664 | 
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			#6  
			
			
			
			
			
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			Well its the lower carb.  However, its not a high speed jet, float level for seat issue, so go figure.   I'm going to look for a replacement and give that a shot.
		 
				__________________ 74 V20 CC with a 150 Johnson (Gone but not forgotten) 89 V20 Cutty with a Tower (Build in process) | 
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