Wellcraft V20 Community

Go Back   Wellcraft V20 Community > Wellcraft V-20 Forums > Repairs
Register FAQ Community Calendar Today's Posts Search

Reply
 
Thread Tools Display Modes
  #1  
Unread 05-03-2009, 09:06 PM
nymack66 nymack66 is offline
God
 
Join Date: Jul 2007
Location: Orlando Florida
Posts: 1,069
Send a message via ICQ to nymack66
Default Looper Shutdown with a rattle noise

Hey guys,
I really need help now big time, I took the Boat out today all was working well, made one stop after a 1/2 hour run at 4 to 5000 RPM, it acted really weird and will not start acted like a dead battery.
Waited a few minutes and she fired right up.
Ran for another 1/2 hour trolling and WOT at times.
Around 4000 RPM when it suddenly started to die down with a loud rattling sound, I immediately shut it down.
I try to start it and its making a rattling sound like something is loose inside and it will not start, I did a compression check on the 1 and 3 cylinder both shows around 60 I am completely stump all the plugs looks ok well oiled it did not overheat since I saw it running at 140 degrees.
Reply With Quote
  #2  
Unread 05-03-2009, 09:59 PM
cterrebonne cterrebonne is offline
God
 
Join Date: Nov 2007
Location: thibodaux, la
Posts: 1,293
Default

Quote:
Originally Posted by nymack66 View Post
Hey guys,
I really need help now big time, I took the Boat out today all was working well, made one stop after a 1/2 hour run at 4 to 5000 RPM, it acted really weird and will not start acted like a dead battery.
Waited a few minutes and she fired right up.
Ran for another 1/2 hour trolling and WOT at times.
Around 4000 RPM when it suddenly started to die down with a loud rattling sound, I immediately shut it down.
I try to start it and its making a rattling sound like something is loose inside and it will not start, I did a compression check on the 1 and 3 cylinder both shows around 60 I am completely stump all the plugs looks ok well oiled it did not overheat since I saw it running at 140 degrees.
60 psi, that doesnt sound good, rattling on a looper probably wrist pin or ring failure. i would pull the head on that side and look for the bits and pieces that are impregnated on the piston.
Reply With Quote
  #3  
Unread 05-03-2009, 10:01 PM
THEFERMANATOR's Avatar
THEFERMANATOR THEFERMANATOR is offline
God
 
Join Date: Dec 2006
Location: Zephyrhills Fl
Posts: 7,206
Send a message via AIM to THEFERMANATOR
Default

Sounds like it leaned out on yeah. Like I was saying in post #2 about your plugs, that one plug REALLY concerned me from the white on it. When you say it acted like a dead battery after a hard run, that is a direct indicator of a stuck piston. Chances are you smeared it when you tried to start it and it didn't kick right off. The rattling is most likely a smeared piston skirt that is rattling against the cylinder wall. Been there, done that. 140 is hot if that is what it was cruising, an old school looper should run 140-170 at idle and IMMEDIATLEY drop to about 100-120 at 3000-4500 and bump 130 maybe 135 under WOT on a hot day. Pull the head on that side and look for signs of aluminum stuck to the cylinder walls, but the head needs to come off.

Let me know if it's bad, my 140 could be made available if it's bad and you don't want to build it.
__________________
2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664
Reply With Quote
  #4  
Unread 05-03-2009, 10:11 PM
Skools Out's Avatar
Skools Out Skools Out is offline
God
 
Join Date: Jul 2007
Location: Graham / Emerald Isle, NC
Posts: 5,926
Default

yep as Ferm said it is shot that 60 psi is a bad sign it should be around 125 psi each
__________________




1978 V20 Cuddy w/ 225 Johnson. And Several other boat's
Reply With Quote
  #5  
Unread 05-04-2009, 09:02 AM
nymack66 nymack66 is offline
God
 
Join Date: Jul 2007
Location: Orlando Florida
Posts: 1,069
Send a message via ICQ to nymack66
Default

Ok I will pull the heads and see what exactly whats going on, Could it be a broken reed? Since I found lots of pre-mix oil in the Air baffle ?
Reply With Quote
  #6  
Unread 05-04-2009, 09:12 AM
THEFERMANATOR's Avatar
THEFERMANATOR THEFERMANATOR is offline
God
 
Join Date: Dec 2006
Location: Zephyrhills Fl
Posts: 7,206
Send a message via AIM to THEFERMANATOR
Default

A broken reed could have done the damage, but they normally window the block when they go through. Remember that a 2 stroke has 2 different compression sides to it, in front of and behind the piston. A compression test only measures in front of the piston and a broken or missing reed won't affect it unless when it broke it went through the engine and damaged the piston or cylinder. Unfortunately though your compression numbers along with the noise is a bad sign, and most likely means that boring and new pistons is in your future. You may be able to clean them with some acid and put just pistons in it, but I'm not normally that lucky. My 140 looper pops at 150-155 pounds of compression, so that should give you an idea of how far down you are. When you pull the heads look for smeared spots on the cylinder walls, that will be the aluminum from the pistons. It is possible on the looper engines though to pull the pistons out with the powerhead still on the mid.
__________________
2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664
Reply With Quote
  #7  
Unread 05-04-2009, 10:05 AM
reelapeelin's Avatar
reelapeelin reelapeelin is offline
God
 
Join Date: Aug 2003
Location: Spartanburg, SC
Posts: 15,610
Default

Another source of a rattling noise could be magnets coming loose under the flywheel...but that would not explain low compression...Ferm's probably right...as usual
__________________
'74 V-20/ BF 150
'95 V-21/ BF 150
'84 V-20/ 200 2.4 Merc
'87 V-20/'18 F150 Yamaha



http://www.wellcraftv20.com/gallery/albums/MJ-hide/Iphone201205.jpg
Reply With Quote
  #8  
Unread 05-04-2009, 11:46 AM
nymack66 nymack66 is offline
God
 
Join Date: Jul 2007
Location: Orlando Florida
Posts: 1,069
Send a message via ICQ to nymack66
Default

Quote:
Originally Posted by THEFERMANATOR View Post
Sounds like it leaned out on yeah. Like I was saying in post #2 about your plugs, that one plug REALLY concerned me from the white on it. When you say it acted like a dead battery after a hard run, that is a direct indicator of a stuck piston. Chances are you smeared it when you tried to start it and it didn't kick right off. The rattling is most likely a smeared piston skirt that is rattling against the cylinder wall. Been there, done that. 140 is hot if that is what it was cruising, an old school looper should run 140-170 at idle and IMMEDIATLEY drop to about 100-120 at 3000-4500 and bump 130 maybe 135 under WOT on a hot day. Pull the head on that side and look for signs of aluminum stuck to the cylinder walls, but the head needs to come off.

Let me know if it's bad, my 140 could be made available if it's bad and you don't want to build it.
Ferm,
Thanks for the offer PM me please with the details and asking price of your 140 I may just install a new motor at this point and keep mine as a spare.
My bad spell never seem to end, Last week Trailer Stolen, I was in the ER two days later with chest pains , now blown looper !
Reply With Quote
  #9  
Unread 05-04-2009, 11:57 AM
reelapeelin's Avatar
reelapeelin reelapeelin is offline
God
 
Join Date: Aug 2003
Location: Spartanburg, SC
Posts: 15,610
Default

Quote:
Originally Posted by nymack66 View Post
Ferm,
Thanks for the offer PM me please with the details and asking price of your 140 I may just install a new motor at this point and keep mine as a spare.
My bad spell never seem to end, Last week Trailer Stolen, I was in the ER two days later with chest pains , now blown looper !

Dang Mack...a bad spell fo sho!!......hope things turn around for you and glad you got outta the hospital standin' upright!!...
__________________
'74 V-20/ BF 150
'95 V-21/ BF 150
'84 V-20/ 200 2.4 Merc
'87 V-20/'18 F150 Yamaha



http://www.wellcraftv20.com/gallery/albums/MJ-hide/Iphone201205.jpg
Reply With Quote
  #10  
Unread 05-04-2009, 12:21 PM
nymack66 nymack66 is offline
God
 
Join Date: Jul 2007
Location: Orlando Florida
Posts: 1,069
Send a message via ICQ to nymack66
Default

Thanks ,
Now this Looper wants to send me right back :)
Reply With Quote
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -5. The time now is 10:43 PM.


Powered by vBulletin® Version 3.8.2
Copyright ©2000 - 2025, Jelsoft Enterprises Ltd.