Wellcraft V20 Community

Go Back   Wellcraft V20 Community > Wellcraft V-20 Forums > Repairs
Register FAQ Community Calendar Today's Posts Search

Reply
Thread Tools Display Modes
  #11  
Unread 09-07-2013, 04:33 PM
BuilderFL's Avatar
BuilderFL BuilderFL is offline
Senior Member
 
Join Date: Mar 2006
Location: Miami, FL
Posts: 455
Default

I was using the wrong O ring at the base of the water pump and it did not go all the way in. Well, I replaced it and it's doing the same thing. Could it be the Sea Foam?
Joe, whats the OMC?
And there is no oil from the lower seal.
Reply With Quote
  #12  
Unread 09-07-2013, 08:49 PM
smokeonthewater's Avatar
smokeonthewater smokeonthewater is offline
God
 
Join Date: Oct 2011
Location: Indiana near louisville Ky
Posts: 1,814
Default

Quote:
Originally Posted by BuilderFL View Post
whats the OMC?
OMC is the parent company, Outboard Marine Corporation, that makes Johnson and Evinrude engines.

I think Joe missed that it was a Mercury
Reply With Quote
  #13  
Unread 09-09-2013, 08:29 AM
BuilderFL's Avatar
BuilderFL BuilderFL is offline
Senior Member
 
Join Date: Mar 2006
Location: Miami, FL
Posts: 455
Default

This is what I'm talking about;

http://i138.photobucket.com/albums/q...ps74f34d04.jpg

http://i138.photobucket.com/albums/q...ps0f689a27.jpg

http://i138.photobucket.com/albums/q...ps15ae11de.jpg
Reply With Quote
  #14  
Unread 09-09-2013, 06:09 PM
spareparts's Avatar
spareparts spareparts is offline
God
 
Join Date: Oct 2006
Location: Raleigh, NC
Posts: 6,192
Default

was there any on top of the water pump housing when you dropped the lower unit?
Reply With Quote
  #15  
Unread 09-09-2013, 08:54 PM
phatdaddy's Avatar
phatdaddy phatdaddy is offline
God
 
Join Date: Mar 2003
Location: south of I-10
Posts: 4,965
Default

builder, you said you replaced the head gskts after the overheat episode, were they blown and water was getting in the cyl or where you just being proactive?

Last edited by phatdaddy; 09-10-2013 at 10:18 AM.
Reply With Quote
  #16  
Unread 09-10-2013, 06:05 AM
kamikaze kamikaze is offline
Senior Member
 
Join Date: Oct 2005
Location: Fredericksburg, VA
Posts: 359
Send a message via ICQ to kamikaze
Default

In my opinion there are two ways to get that much oil. Lower unit is leaking ( view lower unit oil for water intrusion and then pressure test it to verify fix). or your exhaust manifold is purging all the oil/ carbon that had built up in it. I asked about the oil being used as I have found significant oil purging from the exhaust after overheating a engine if the oil has a decarb / cleaning additive. And the oil you show is more grayish than rainbow stained indicating he oil has already then burnt. I agee with Phat, Pull the spark plugs to verify no water intrusion in clyinders after head gaskets install (will also purge exhaust). If not and the lower unit pressure checks go run it and see if it cleans up.
__________________

74 V20 CC with a 150 Johnson (Gone but not forgotten)
89 V20 Cutty with a Tower (Build in process)
Reply With Quote
  #17  
Unread 09-10-2013, 09:05 AM
smokeonthewater's Avatar
smokeonthewater smokeonthewater is offline
God
 
Join Date: Oct 2011
Location: Indiana near louisville Ky
Posts: 1,814
Default

have you done a compression test on this engine?
Reply With Quote
  #18  
Unread 09-15-2013, 01:20 PM
BuilderFL's Avatar
BuilderFL BuilderFL is offline
Senior Member
 
Join Date: Mar 2006
Location: Miami, FL
Posts: 455
Default

Guy, no water in the plugs and compression is all within 5 psi (110-115) and I am almost certain that it had more to do with the Sea Foam and purging old carbon than anything else. All the grey stuff is gone but I cant get her to idle correctly. Since Im back on the road my mechanic is picking up the boat tomorrow and will take a look at it. I will post results as soon as I hear back from him.
Thanks for your input.
Reply With Quote
  #19  
Unread 09-17-2013, 02:17 AM
bradford's Avatar
bradford bradford is offline
God
 
Join Date: Nov 2006
Location: Wilmington Island, Georgia
Posts: 4,879
Default

Hope it works out to something cheap for ya builder!
__________________
1985 Wellcraft V-20, Evinrude ETEC 150: SOLD
1979 Marine Trader 44, twin Ford Lehman 120s
2006 Panga 14, Tohatsu 20
Reply With Quote
  #20  
Unread 09-20-2013, 08:47 PM
BuilderFL's Avatar
BuilderFL BuilderFL is offline
Senior Member
 
Join Date: Mar 2006
Location: Miami, FL
Posts: 455
Default

$580 later, the old trusty 1988 Merc 200 is back to running sweet.
The whole grey stuff was the sea foam cleaning whatever was inside the motor, so the lesson here is, when trouble shooting, do one thing at a time only. It was all carbs...they replaced the gasket kits, valve kits (not sure what this is) and a new pump diaphragm. Parts was $142.10 including $25 for picking up the boat and $405 for 4.5 labor hours.
What do you guys think about the bill amount? Fair or over the top?
As always, my thanks for all your input and support and I guess I should stick to my architecture and try to lay off the mechanic in me. Not! My favorite uncle was a car mechanic, was working with him since I was 14 till I went off to college and I really enjoy it, plus I've made a significant investment in tools. Just wish I had more time to work on the boat, the old truck, the spare motor...but I need a plan to get rid of the bills that just keep coming in every month before I can stop working (the jobs that actually pay).
Fishing tomorrow at 6am. If I'm lucky you'll get pictures
Reply With Quote
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -5. The time now is 08:55 AM.


Powered by vBulletin® Version 3.8.2
Copyright ©2000 - 2025, Jelsoft Enterprises Ltd.