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#1
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well? we are waiting?
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#2
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All right here is the skinny, left Cape May at 1100. Boat running beautiful.
We ran into quartering seas 2-4's quick duration and a lot of chatter on the radio of guys heading in to fish inside etc. Senor Bertram just cut right through. It was wonderful. Ran for about four hours, Got up about six miles north of Barnegat Inlet and then the port engine started acting weird. Tach and engine revving up then dying back, would not stay at upper rpm. Shut her down and got down to investigate. Found that the fan belt was so loose on the alternator pulley that I could spin it around with my hand. Tried to start engine, no battery juice. Apparently was running on battery voltage the whole way. They were fully charged group 27's. Tried to use the parallel switch to start, battery was too dead. All I got was clicking from the starter. Called Tow Boat U.S They got out there and we used their battery and jumper cables and the engine started right up. Idled fine for a few minutes, went up to the bridge and revved it and sounded good. Oh, two things, while I was waiting for tow Boat I got down and adjusted the pulley and got the belt tight. and also the engine did not over heat as we were looking at the gauges the whole time. So we were going to run the boat the last forty miles and said good bye to the Tow guys. Got on plane and it started the same thing again. Called the Tow guys on the radio they were still right there. We tried to see if we could jump from the good battery on the boat to the bad battery and we ran the good engine while hooked up and tried to charge the bad one for a few and I saw some rubber smelling smoke come out very light from around the starboard engine area. Don't know if the jumper cable was touching something hot or what yet. Told the Tow boys to bring us in. Called Capt. Pete and he told me to have it towed to Manasquan and his marina, that is where it sits right now waiting for today and their head mechanic to check it out. Went down Sunday and changed out the bad battery and the engine started right up. Alternator pulley is chirping away and the alternator is NOT charging the battery according to my meter. I believe I ran on battery power for about four hours before she finally died. Capt. Pete stopped by to see me at the boat, I hooked the boat up to shore power and am waiting today to talk via phone to the mechanic. Wish me luck.
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Willy 1986 V20 Old School 1992 V20 1992 150 Yamaha 1997 HydraSport 2250 Vector 2009 17' G3 Outfitter "G Spot" http://www.youtube.com/watch?v=TDebw...eature=related "I won't be wronged, I won't be insulted and I won't be laid on a hand on. I don't do these things to others and I require the same from them" JW |
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#3
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I was wondering if you made it back to land, you didn't answer the last time I called you, good to hear you've got everything under controll
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#4
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Damn Willy, sorry to hear of your problems with the boat. The good side is that it seems whatever the problem is, it isn't the engines themselves.. they sound like they were running good, and the fact that they started right up each time is a good sign. I'm sure that everything is in good hands, but if there's anything I can do to help just give me a holler.
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1987 V20 w/1987 150HP Yamaha on a Shoreland'r Trailer 1978 16.5 Airslot w/1996 120HP Force on a Four Winns trailer 1996 V21 w/1993 200HP Mercury on a Shoreline Trailer All towed by a 5.7L Hemi Durango. If God didn't have a purpose for us we wouldn't be here, so Live simply, Love generously, Care deeply, Speak kindly. (Leave the rest to God) ![]() Silence, in the face of evil, is itself evil. Not to speak is to speak, not to act is to act. God will not hold us guiltless. |
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#5
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Thanks destroyer, so anyhow here is the skinny as of today.
The mechanic says that the raw water pump has a leak, it is actually shot and needs to be replaced. Apparently it was spraying a small amount of sea water on the alternator and just shorted and corroded it out. Needs a new raw water pump, needs the alternator rebuilt. I am having Capt Pete and his buddies go over both engines and repair what is needed. There getting started today, and are then going to run it under load and check it all out and then give me a call. Hopefully I will be up and running in a day or two. A few hundred dollars poorer but I am glad there is nothing major wrong. then I got to get someone with me and go to Point Pleasant and pick her up and bring her home to Raritan Bay. About 55 miles by water.
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Willy 1986 V20 Old School 1992 V20 1992 150 Yamaha 1997 HydraSport 2250 Vector 2009 17' G3 Outfitter "G Spot" http://www.youtube.com/watch?v=TDebw...eature=related "I won't be wronged, I won't be insulted and I won't be laid on a hand on. I don't do these things to others and I require the same from them" JW |
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#6
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.........a three hour tour.....a three hour tour........
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1986 V-20 1986 Yamaha 150 HP |
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#7
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I'll meet you there in my V- with the little wheel, just in case you need a tow. LOL That is an Adventure, glad it wasn't too costly..
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1996 -19' NV Flats 115 Mercury 4-stroke 1983 -20' Wellcraft Center Console 250 XS |
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