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  #11  
Unread 07-06-2008, 05:23 PM
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Quote:
Originally Posted by BigDaddy View Post
Answer the question,please. How much for a diagonstic?:D
I'm fair and reasoneable with everybody, I keep getting told I work for too little by friends who work for themselves. The main issue would be the distance between the 2 of us though, I'm almost 4 hours away from FT LAUDERDALE. What kind of problems are you haveing?
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
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  #12  
Unread 07-06-2008, 06:03 PM
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Long story short, when I bought the boat (consignmeht dealer) they told me to keep the oil tank 2/3 full, dont fill it all the way. No problem, I thought, filled the tank 2/3 full on our first outing and kept my eye on it. Here in, lies the problem, after we were trolling in the ICWW one night (with the baby, no doubt), we were ready to call it a night and go home-4.5 miles away-i decided after the rods were put away I would give it a little gas, being i had never had it over 1/4 throttle. Well, after getting all the rods put away and getting straight, I slowly gave it about 1/3-1/2 throttle, it took off like a jet. Right as we were planing out, the motor died. We were dead in the water for about 2-3 minutes before it would fire back up. When I did get the motor started again, we developed a "tick". It wasnt a "knock", but a tick. We limped home and thanked god we made it safely. After 50 Gal of gas or so, since we bought the boat, it donned on me I hadnt burned a gallon of oil. There ya go, although the entire 50 gallons of gas was in a "minimum wake" zone, and being I was a new skipper, I didnt want to push anything (until I was familiar with my new vessel), we cruised it everywhere-up and down the ICWW. Would you like to hear the "tick"? I know its not good, i just hope its not BAD.

I cant stand to think that the "Reel Lucky" is not real lucky.
What you think?
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  #13  
Unread 07-06-2008, 06:04 PM
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Dont worry, Ill bring the boat and the BEER
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  #14  
Unread 07-06-2008, 06:23 PM
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I take it your alarm doesn't work? How about the reservoir on the engine? Is it empty? I know the early YAMAHA's had an upgrade on the oil injection pumps as a few lost the powerheads due to failed pumps. If you got a noise then chances are your going to need to tear it down to find out what is making the noise. From your description best case scenario would be a scuffed piston, this would cause your tick which would actually be piston slap. So then you would have to decide is the engine worth putting that much money into to rebuild it? I can go out and take some pictures of what a YAMAH with a failed oil pump looks like, it aint pretty. And the cost to repair that 250 was more than I could re-sell it for after building it. It sounds like at this point a compression test is in order, and then pull the heads to see what it looks like inside.
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
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  #15  
Unread 07-06-2008, 06:35 PM
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Piston 1 is where the "tick" sounds like its coming from, 125 psi.
Other 5 pistons are at 135 psi. I syphoned all 50 Gallons out and have mixed 10 Gal worth. I was told to put an ounce of oil in each cylinder and turn the engine over (to circulate the oil) after doing that 3 times the "tick" has gotten quieter, but still I worry.
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  #16  
Unread 07-06-2008, 08:44 PM
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Sounds like a smeared piston. Reduced compression with a tick is a sign of a smeared pistom in the ring area. Haven't ever been in one of them old YAMAHA's, so I'm not sure if you could snake it out without splitting the case. If you could get it out without splitting it, you could do a light honing to clean the aluminum off the cylinder and replace the one piston to get it running again for awhile. On an old outboard like that I wouldn't personally sink alot of money into it since you don't know the history on it. Could be able to do just a piston for $200-300 if it isn't in that bad of condition inside. If it's all slated up from years of saltwater useage, then it can get expensive when you have to hot wrench everything apart.
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664
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  #17  
Unread 07-06-2008, 10:15 PM
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Been there done that!! I had 1989 Yamaha 175 and the injection pump let go, sounds nasty when you are going along!!
I really nursed it along to get home, just idle all the way! Comression in one cylinder was junk and needed one pistion. I sold the motor and bought another.

fix it and get rid of the oil injection!!
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  #18  
Unread 07-07-2008, 09:35 AM
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Another case showing the merits of premixing.
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  #19  
Unread 07-07-2008, 06:06 PM
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Well the first thing I did was rip out the oil tank. Second thing I did was syphon out all the gas (50 Gals), mixed it up and poured it back in. I shot some video with sound last night so you could hear what it sounds like. Im gonna start a new thread with the video tonight.
Firm believer of B.O.A.T (break out another thousand)
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