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#1
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Well now you show up!! Just kidding!
Well besides thge 2500 RPM thing, all the wires on the motor are soft and as we took the tape off them there were all kinds of breaks and green wires. Also some one had lots of conections spiced in. So the wires had to get done!! The shift assembly were the shift intrup is also wore so bad that it would not shift right any longer and I had to have it welded. And reverse still isn't all that great. The water pump is peeing real slow and there is water coming out the front of the mid section near were the steering arm bolts. Its a pretty bad leak, so bad that I think water must be getting to the drive shaft and rusted it in to the motor, as we can't get the lower unit off! I mean we jumped, kicked. wedged, pryed, hit with a hammer that thing is on there solid!! The compression has always been perfect in the 90's all 6 cyl. And when it was running this whole summr it ran great!! I guess what I should have done was to take and got the spare motor going, but that had a bad lower unit and bad eletric also. So with all the things going on with the motor I have decided that the best thing to do is move on to another motor. The Merc just happened to show up at the right time for the right price. And belive me after buying the house and all the toys I got for the boat over the winter I don't have a spare penny around here!! I had too beg borrow and steal to get this merc! So wish me luck on the Dark Side! Therm, no more vacations during the fishing seasons, you might have perveted me from going to the dark side! Its all your and skools fault for not being there for me!
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#2
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MJ, being that thing is leaking water in those locations, it more than likely has corroded the spline locations at the lower bearing of the crankshaft and the shaft to the foot. It was probably caused (by the last owner) from improper alignment of the waterpump tube or it has rotted a hole in it.
I've fooled with one motor that was sunk for a period of time and it was a real SOB to remove. The wedges and bumping of the propeller engauged over a period of days finally released it. Sorry you went black.
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'75 Cuddy with '00 Johnson Ocean Pro 150 horse Benny |
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#3
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Man, MJ, is this not the third engine you are now on in less than a year? I hope this one works out well for you.
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#4
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MJ - If you don't like it . . . I'll buy it back from you :)
This was my dad's boat for 15 years . . . 25ft steigercraft with a 2.4L 200hp. 10.5 gph @3800 with a 15 pitch prop. It would top out at 5800rpm loaded. On a flat calm day it would just touch 40mph. The motor was still running strong when he repowered in 2001.
Last edited by bigshrimpin; 07-24-2008 at 08:08 AM. |
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#5
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This was the first motor I ran on this boat.
But the Wellcraft went Thur a few 165 I/O, raw water cooled, rotted from the inside out 175 Yamaha, Oil injection failed 2nd 150 Yamaha was junk when I got it, 175 Evinrude that I sold with it. I really need to buy NEW but just can't swing the cash, and what a shame to spend $15,000+ for are short season! I am sure I will be fine this time around, I can feel it! BS gong to take care of me!!
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#6
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Sell the boat now!!!!!!!!!!!!!!!!!!!!!!
Get out while you can!!!!!!!!!!!!!!!!!!
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Heavily medicated for your protection. |
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#7
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should have told me that 15 years ago!!!
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#8
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You are so close to fix the Rude ..I have a v6 lower unit if you need it fix the darn engine it will last ..Good luck with the new engine , fix this Rude for spare , so when Ferm is on the road again you use the spare until he's back !
As for going to the "dark" side now you can compare !! |
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#9
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[QUOTE=nymack66;125442]You are so close to fix the Rude ../QUOTE]
NYMack - You should see that motor . . . The motor is on it's 10th life. The only way that it'll survive is with a donor mid and lower and all new ignition and harness . . . and it's a BIG "if" whether the lower will drop. It's a total rehab . . . I wish it weren't. MJ is getting the motor with controls and prop mounted and rigged for $600 + the piles of aluminum scrap ;) Last edited by bigshrimpin; 07-24-2008 at 01:24 PM. |
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