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  #21  
Unread 05-04-2009, 09:58 PM
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You need to find where your compression was leaking. Broken reeds will not cause low compression unless something is jamming them closed and not allowing any air past.
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  #22  
Unread 05-05-2009, 09:09 AM
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Please see the flywheel photos on this link http:\\www.nymack66.com
As for the flywheel been loose I will check since I did pull it off last year !
What is the correct procedure for a compression check I disconnected the fuel line remove left 3 plugs in and connected to one cyl crank the engine about three turns. Is this correct?
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  #23  
Unread 05-05-2009, 09:40 AM
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9 amp charging so not a magnet issue. you could pull the carbs and look at the reeds or heck pull the reed body and look in the cylinders and turn by hand till each rod is at the hole then rock to see if you have a bad rod bearing or loose rod cap. those rod caps use either a 5/16 or 8 mm 12 point socket. must be a 12 point. you can check the torque of the rod cap bolts threw the reed holes as well. that 12 point 8mm is avail. at sears.
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  #24  
Unread 05-07-2009, 09:00 PM
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Guys,
Why is it the pistons are really loose ? Is this normal ? Is it possible the previous owner installed the wrong set of pistons in a re-bore sleeves?
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  #25  
Unread 05-08-2009, 01:49 PM
Steplift 72' Steplift 72' is offline
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Originally Posted by nymack66 View Post
Guys,
Why is it the pistons are really loose ? Is this normal ? Is it possible the previous owner installed the wrong set of pistons in a re-bore sleeves?
The pistons should not be "really loose" but they will slighly rock. I had a rattling 86' model 140 looper that still had 125 pounds of cranking compression. It turned out that a series of motors in 86' had carbs that ran the motors too lean, mine was one. In the first 6 months it had lost 400 rpm and sounded terrible. The piston tops and cylinders looked perfect but the lean running had worn the motor out in a couple hundred hours.
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  #26  
Unread 05-08-2009, 02:14 PM
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85 had ALOT of problems with the 140, and 86-early 87 did as well as far as carbs go. If you run the VRO they aren't too bad, but if you pre-mix it makes it worse MUCH WORSE! I spent several days re-jetting my carbs after I swapped from the early style 140 carbs used in 85 only to those that were used in 86 and the first of 87. The domes will be loose, but it's the skirt you have to worry about. If the piston skirts are loose the engine could have decent compression and still not idle. I was gonna mention that your pistons looked awfully loose from your pics, but it's hard to judge from pictures if they are too loose or not. OMC issued a bulletin though to jet up 2 sizes in the mains on the early loopers as the aggressive porting in them caused ALOT of lean out issues.
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2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
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  #27  
Unread 05-08-2009, 02:30 PM
Steplift 72' Steplift 72' is offline
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85 had ALOT of problems with the 140, and 86-early 87 did as well as far as carbs go. If you run the VRO they aren't too bad, but if you pre-mix it makes it worse MUCH WORSE! I spent several days re-jetting my carbs after I swapped from the early style 140 carbs used in 85 only to those that were used in 86 and the first of 87. The domes will be loose, but it's the skirt you have to worry about. If the piston skirts are loose the engine could have decent compression and still not idle. I was gonna mention that your pistons looked awfully loose from your pics, but it's hard to judge from pictures if they are too loose or not. OMC issued a bulletin though to jet up 2 sizes in the mains on the early loopers as the aggressive porting in them caused ALOT of lean out issues.
I tried to run the VRO, but while breaking in the new powerhead supplied by OMC, the oiling system on the other motor fouled up and quit working. Thankfully there was 50-1 in the tank for break in. I gave up on the VRO at that point, it alarmed when idling up to the dock after better than 6 hours running without consuming a drop of oil! I've used pre-mix on every motor since. Never another problem with those motors, I believe that aggressive porting must have been very efficient....they really performed and the pair used 15 gph at 4000 rpm with 17p SSTII's. Those 97' model loopers I had ran no where near the early model motors.
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  #28  
Unread 05-08-2009, 03:08 PM
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Quote:
Originally Posted by Steplift 72' View Post
I tried to run the VRO, but while breaking in the new powerhead supplied by OMC, the oiling system on the other motor fouled up and quit working. Thankfully there was 50-1 in the tank for break in. I gave up on the VRO at that point, it alarmed when idling up to the dock after better than 6 hours running without consuming a drop of oil! I've used pre-mix on every motor since. Never another problem with those motors, I believe that aggressive porting must have been very efficient....they really performed and the pair used 15 gph at 4000 rpm with 17p SSTII's. Those 97' model loopers I had ran no where near the early model motors.
Yep, the 85-87 had the small 3.5" bore in them and the porting was pretty aggressive in the intake, but they had a BIG exhaust that was VERY efficient at cruise and up. The early motors were a bit doggy off idle and the 85 was pretty dead until 3600, but once the R's were up they would RUN. Another BIG issue with the early engines was the carbs and the fact that it was a completely new design for outboards, let alone new for OMC in general. The plastic carbs with aluminum bases became standard after that on loopers, but up until 85 it was brand new and not really tested much. Once you get the jetting down though they are GOOD on fuel and perform pretty good. And it seems like ALL of these loopers like a little different jetting once broke in.
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2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664
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  #29  
Unread 05-11-2009, 12:22 PM
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Default Found it

The lower connecting rod number 4 cylinder was almost completely loose on the crank, it spun the bearing 1/2 inch off and froze to the crank, melted the bearings and was at the point to break free!
At this point I will swap in a re-build power head, the previous owner of this engine was one loose cannon base on issues I had with this engine, wrong lower unit now this.
I will post the pictures tonight.


Last edited by nymack66; 05-11-2009 at 08:36 PM. Reason: Photo
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  #30  
Unread 05-11-2009, 08:42 PM
Steplift 72' Steplift 72' is offline
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Quote:
Originally Posted by nymack66 View Post
The lower connecting rod number 4 cylinder was almost completely loose on the crank, it spun the bearing 1/2 inch off and froze to the crank, melted the bearings and was at the point to break free!
At this point I will swap in a re-build power head, the previous owner of this engine was one loose cannon base on issues I had with this engine, wrong lower unit now this.
I will post the pictures tonight.

I don't guess you can blame everything on VRO......but were you running the injection or pre-mix? Wrong lower unit??
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