Wellcraft V20 Community

Go Back   Wellcraft V20 Community > Wellcraft V-20 Forums > Performance

Reply
 
Thread Tools Display Modes
  #1  
Unread 05-09-2019, 09:43 AM
Blue_Runner's Avatar
Blue_Runner Blue_Runner is offline
Administrator
 
Join Date: Aug 2004
Location: Lexington, North Carolina
Posts: 9,234
Default

I agree with Destroyer. Could it be that when you hit the sandbar it damaged the female connection where the splines lock in and it is slipping there? Not sure what it is called. Or your marks on the prop just coincidentally lined up? Keep us posted on what you find out.
__________________

1994 Wellcraft V21
Reply With Quote
  #2  
Unread 05-09-2019, 08:10 PM
phatdaddy's Avatar
phatdaddy phatdaddy is offline
God
 
Join Date: Mar 2003
Location: south of I-10
Posts: 4,965
Default

are you judging rpm increase by sound or actual tach readings
Reply With Quote
  #3  
Unread 05-09-2019, 08:43 PM
Rusty5387 Rusty5387 is offline
Junior Member
 
Join Date: Apr 2017
Location: Toms River, NJ
Posts: 18
Default

Thanks everyone! I am judging it based on sound and on my tach. I will see if I can find a prop to test with before I go out and buy one. The other thing that was brought up to me was to make sure when we installed the new lower unit that it had a ventilation ring already installed or was I supposed to transfer that from my old lower when I took the prop off. A friend of mine had an issue with their ventilation ring and it caused the same issue on their outboard. Fingers crossed that's but I won't be able to check until sometime tomorrow.
Reply With Quote
  #4  
Unread 05-10-2019, 06:10 AM
phatdaddy's Avatar
phatdaddy phatdaddy is offline
God
 
Join Date: Mar 2003
Location: south of I-10
Posts: 4,965
Default

I was just asking because a wacky tach is also a symptom of electrical/charging issues.
Reply With Quote
  #5  
Unread 05-12-2019, 08:47 PM
THEFERMANATOR's Avatar
THEFERMANATOR THEFERMANATOR is offline
God
 
Join Date: Dec 2006
Location: Zephyrhills Fl
Posts: 7,206
Send a message via AIM to THEFERMANATOR
Default

Make sure the shift linkage is adjusted correctly. Not sure on the yamaha, but on OMC's you have to set the shift shaft height. If you don't get it correct, it will jump out of gear like you describe, and it trashes the clutch dog when it does it. Also on that vintage yamaha, make sure the shift shaft isn't rusted out to nothing. They can rust to the point tbey twist, and not hold it in gear.
__________________
2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR

2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
http://www.wellcraftv20.com/communit...ad.php?t=11664

Last edited by THEFERMANATOR; 05-12-2019 at 08:55 PM.
Reply With Quote
  #6  
Unread 05-13-2019, 05:32 PM
Rusty5387 Rusty5387 is offline
Junior Member
 
Join Date: Apr 2017
Location: Toms River, NJ
Posts: 18
Default

I appreciate all the help guys! At this time I am pretty sure its the ventilation ring. I spoke with the company I got the new lower unit from and they confirmed it did not come with a ventilation ring and I checked the old lower unit and it has a ventilation ring on it so I just need to figure out with ventilation ring I need and where I can purchase it from. Once I install that I will update if it fixed the issue or not.
Reply With Quote
  #7  
Unread 05-22-2019, 10:00 PM
Rusty5387 Rusty5387 is offline
Junior Member
 
Join Date: Apr 2017
Location: Toms River, NJ
Posts: 18
Default

Okay I believe the problem is solved. It was not the prop and there is no such thing as a ventilation ring for a Yamaha outboard. Before launching the boat this spring I added an underwater light that I've been wanting to add for a few years now. Instead of purchasing a light that I would have to mount to the transom I opted for a light that screws into your existing drain plug. The light worked great, was very bright even in the darker water in the river near me and attracted bait fish to the boat almost immediately. I realized that is the only thing I changed on the boat this year prior to having the issue. We pulled the boat out and it looks like the light sticks out just enough to mess up the clean water flow that should be going right to the prop. I removed the light and put the regular drain plug back in and took it our for a quick run. The boat got on plane much quicker and ran great. I could not get it to ventilate again or a jump in the rpms. I appreciate the advice from everyone that replied but turns out it was my own fault. tight lines guys
Reply With Quote
Reply

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -5. The time now is 11:33 PM.


Powered by vBulletin® Version 3.8.2
Copyright ©2000 - 2026, Jelsoft Enterprises Ltd.