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#1
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I found a link to outboardbooks.com from the Johnson website. I found it there. Thanks.
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#2
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I would try spinning the fly wheel and see if that piston is moveing.I,ve seen where a cylinder had no compression and the rod be blown and the engin still run
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#3
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That white t-stat housing I'm betting was the cause of the failure. OMC changed out those white housings to a black housing in 87-88 due to problems with the white ones sticking and overheating. That engine looks to be LOOSE to say the least from the looks of the lower cylinder. Personally I would reccomend finding a good used engine Vs rebuilding that one. Speaking from experience, the 85 is a nightmare to try and get to run decent, and it will always be on the ragged edge of living unless you do ALOT of upgrades to it. 85 is a one year only set-up, and tthey just aren't really feasable to keep alive. Look for an 88+ 140 to replace it with.
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD ![]() AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664 |
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#4
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Well, DAMN!!! Not much more I can say but, DAMN!!! Guess I'll be content with the stuff I actually bought the boat for. Trashing a running motor seems so wrong. LOL
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#5
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Yeah. I'm nowhere near ready for a motor anyway. I have plenty of time. Just would have been nice to cross it off the wishlist. I appreciate all the info and suggestions.
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