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				__________________ 2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD  AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664 | 
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 Thanks again for the info. 
				__________________ 93 V-21 200/9.9 Yamaha | 
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			Yes I purchased the engine newly rebuilt, in Sep, 2010 I was told that when he got the engine in off of another boat he  opened it up there was nothing wrong, he changed the crank and rebuilt it anyway, but I have a problem trusting this guy having the problems I have had so far, I know he just slapped used parts on it to get it working, it has been running O. K. felt like I was a little week on power though. My past posts have told about my RPM / MPH issues. I don't really know what to do next ? Thanks for everybodys responses.
		 
				__________________ Tight Lines !! | 
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			#4  
			
			
			
			
			
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			normally there are two different head gaskets available for Johnrudes, ones thicker than the other to drop compression for commercial use, some one could have replaced a head gasket at some point
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			never mind, I see thats its a 60 degree motor, I think they use orings. Check the casting numbers on the head and make sure they match
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			I went down today with fresh gas, checked in-line filter inside motor, looked good,checked all plugs, sprayed them with carb cleaner, disconnected fuel line from engine side of primer ball and pumped a gallon into a bucket, it looked perfect, hooked line up to 6 gall. tank, it started right up using the fast idle lever, let it run for about 1 min. RPM's showing about 1500, pushed the fast idle lever down, she kicked like a mule and shut, couldn't get it started again. I don't know, maybe the fuel pump ? any suggestions ?
		 
				__________________ Tight Lines !! | 
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			#7  
			
			
			
			
			
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			If it were the fuel pump you ought to be able to mash the primer ball hard enough to fill the fuel bowls and keep it going.  I lean toward fuel because it died off when you decreased the fast idle.  My motor did something similar a little while back.  It would idle for a while and shut off but the primer ball didn't feel right.  It was kinda squishy and never felt firm like it does when the needle is in the seat.  I didn't discover the primer ball was bad until after I took the fuel pump off inspected it and  put it all back together.  Went to the local marina and purchased a primer ball, installed it in minutes and cured the issue.  The old one had a faulty check valve even though it would still move some gas when tested.  I left the old one in the splashwell, it hardened up like a piece of plastic. I say ethanol finished it off as it was nearly 10 years old.   Hope you don't mind but I got a question for the gurus about your motor. Assuming all the jetting is the same in the carbs wouldn't having one side lower by 20 psi cause a bit of a nightmare on tuning it to idle smooth? Is there idle air adjustments or something? 
				__________________ 1996 -19' NV Flats 115 Mercury 4-stroke 1983 -20' Wellcraft Center Console 250 XS | 
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