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#1
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CB
![]() Ok BS came by today and just left. We found that one ck vale in the fuel pump was sticking so we changed it out, seems fine now. There was no metal shavings of any kind on the pump screen so i guess they never got by the Racor. We had a hose getting kinked some when the linkage was at wot and we fixed that also. We drained the bowls but did not do the test you said as I did not read this before hand. Plugs are pretty dirty and replaced. The motor starts like a dream and idles fine!! BS felt the water and said I am good to go! I still hate how hot it is but everyone says its good then it must be! When we had the carbs off before we cleaned the crap out of them and set the floats, and reinstalled, and since tere was nothing on the pump screen I am sure they are still that way, At least I hope so?? We really don't think its a fuel issue at this point?? But I have not put the boat in the water yet to see if anything we did today helps?? I will try to get out tomorrow to test it and see, I will also try your test to see if it is something there. When I came down to plane before it would clear up and when I gave it gas it would started immediately again. But waited to start for a mile or so when it would first show up. I am hoping it was something we fixed today?
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#2
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O yea only happens at high rpms, 4000 and above. when it happens I lose 1 to 500 rpms, mostly it starts losing 100 and goes to 500 as you go. I just give more gas to get them back up but still sputtering.
see what happens tomorrow? Thank
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#3
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Does it eventually smooth out and sound like it has lost a cylinder? This sounds an awful lot like a fuel issue where your losing one cylinder. Although it could easily be a switchbox or stator issue. When it does it next time shut it down while it's doing it and go back and pull all of the plugs out. Look for the one that looks like it's not firing or out of the ordinary. If they all look uniform, but the problem is still there I would suspect the stator's high speed side. If one of your plugs looks really light in color then you know which carb to check. If one plug looks wet or fouled then check the ignion for that circuit. You need to isolate the problem so you know which are to address.
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2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD ![]() AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664 |
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#4
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Will do!! I changed all plugs today, so they are all new now, they were a bit oily and looked old?
This is a response I got from Iboats. I explained all just like I have done here, but I think this guy is wrong as I had this issue long before I went trolling for Tuna. I am going again by th way Wednesday!! Quote:
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#5
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MJ - I thought you hadn't run the boat since we went out around wings neck. There were two lil' hicups on take off, but it never hesitated or lost power during the 2 hour run (after we replaced the stator) . . . unless you dropped some roofies in my soda :) and missed something. I anxiously waiting for tomorrow update. Hope all goes well . . . if the Tuna are around . . . I going out this weekend.
Those plugs you showed me today were dripping two stroke motor oil :) |
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#6
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BS you smoking anything??
I just told you I caught a Tuna last wed, and that I went for a ride in the boat Sunday, so how could the last time I took the boat out be in July with you??
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#7
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He needs to open the door to the shop when he's test running those motors. Breathing too many fumes.
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Heavily medicated for your protection. |
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#8
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Quote:
Hey . . . did you get out today? I'm dying to know. |
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#9
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I am leaving here at 4am, I can't wait!! A guy I know went today and they caught another 150 ponder out there today!
Also yesterday on the Chatam side they caught a 1200 ponder!!!! They say the big ones have been close and that there is at least five 700 ponders this past week!
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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#10
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Well the bad news first, 6 footers out there wind and waves in are face, after 2 miles turned around and came back in, NO Tuna
![]() Good news, came in and went out in a different area, drove boat about 15 miles at about 5000 rpm doing any were from 25 to 29 knots Opened it up and topped out at 33 knots, Motor never missed a beat!! Could have trimmed it a bit more and got another mile an hour?? So after putting new plugs, new ck vaule in the fuel pump, and redirecting the supply hoses to the carbs, it works! Not sure what fixed it?? Redistricting the fuel hose was like this, it had one supply hose from the pump, across the motor to the other side and that one hose went to top carb, then from there each carb feed off the one above. Now there is a 3 way on the pump and a hose going to each carb direct. So was it the hoses?? Ck Vale? plugs? or a combination of? But it works!! Thanks all and to BS for stopping by to help me out!
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1986 V20 ![]() Old Fishermen never die, we just SMELL that way!! |
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