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  #1  
Unread 11-08-2008, 01:19 PM
randlemanboater randlemanboater is offline
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How'd you get metal shavings in your gas?
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Unread 11-08-2008, 03:45 PM
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Well I took the boat for a long ride and still have the same issue t times??

Quote:
then push the key in to chole the motor, if it picks up, you have a fuel issue between the fuel line and the intake, if it bogs down when you push in the key switch, it sounds electrical
when I pushed the key in, it bogs down and stalls if I hold it there long enough??

I am also still worried about how hot this thing is?? Even at a 7 miletun at 4500 rpm's as soon as you slow down seconds after there is steam coming out?

Did I say I love Merc's yet today
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Unread 11-08-2008, 04:11 PM
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The steam isn't a big deal MJ, get a temp guage and check it. Anything under 170 is pretty well normal for a MERC at low RPM's. Even my EVINRUDE in 65 degree temps will have alot of steam coming off the water from the piss tube. Sounds like you need to get BS over for a ride though.

Have you had the cowlings off of the engine yet? Check it for any restrions or such in the cowling or by the carbs. You may have an air blockage to the engine causing it to run rich since you said pushing the choke bogged it down. Theres also a chance you have some trash caught in one of your needle and seats causing this since all of the debris you mentioned in your filter. How do the plugs in it look? Try running it in the water under load and shut it down while your running on plane. Then go back and pull the plugs out. This will help you to figure out if you have a cylinder loading up or not.
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Unread 11-08-2008, 07:28 PM
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what exactly did it do today, leave the temp issues out of the description( I agree with Ferm, doesn't sound liek anything is wrong there). it doean't sound like its runnig rich, sound more like an intermittant ignition issue, but with out running it myself, it would be hard to tell
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Unread 11-08-2008, 08:18 PM
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After finding the metal shavings in the filter I was thinking this was the problem? So I drained the gas from the filter to see if there was any water, there was none.

Took it for a ride, started right up, and we idled out of the harbor. Got pass the no wake area and opened her up, she went fine for like 2 mikles or so. Then I could feel her sputter a little and lose rpm's
At first I was thinking that maybe the shifter was backing down its self, but that was not the case.
drove out about 6 miles and it was sputtering on and off the hole way. Got out to a light house were some guys were fishing for tog, shut her down while I asked how the fishing was, They said it sucked and I wasn't missing anything!

So I started her up and she was on like a light switch and off we went. after about 1 mile we started the process all over again?? Then I remembered about the key switch, so I pushed it in and it got worse, I held a little long at one point and stalled the motor.
Started her right up and came the rest of the way sputtering all the way.

It would go again for a few seconds then it would start breaking up again, after a few min it would go good again then replete.

Thanks guys
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Unread 11-08-2008, 09:49 PM
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go back thru the fuel system again just to be on the safe side, pull the carbs down and blow them out again, you might have picked up some trash. Make sure you check the float levels(been there, done that), make sure they are not too low. Once you fell the fuel system is ok, take a hard look at the stator, sound like the high speed windings may be going out. I know you and BS swaped out a bunch of the ignition earlier, was that new stuff you ended up with on it? Oh, and don't forget to check the things we all forget about, battery cables, ground connections, harness conections, kill switch, etc.. BS, you got another boat harness you can plug into the motor to eliminate the harness side/kill circut?
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Unread 11-08-2008, 11:10 PM
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Sounds like MJ needs to start with step #1 of engine diagnostics. Get you a remote tank and hook it up with 5 gallons of fresh gas and see what happens. This way the shavings and possible fuel restriction can be eliminated. Drain the float bowls and try to catch it so you can see if metal made it that far. The metal in the filter makes me think you have debris in the anti-drain back valve(if you have one) or something in the fuel pick-up tube.
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2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD

AND THE PINK JEEP!!!! R.I.P.
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  #8  
Unread 11-09-2008, 07:39 PM
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Can someone pass me a gun PLEASE!!!!!!!!!!

Long story short I have no gauge hooked up. Does anyone know the right wire for the temp?? BS said Tan or Tan with Blue strip?? he wasn't sure??
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