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Unread 06-01-2008, 11:09 AM
cfelton cfelton is offline
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Join Date: Dec 2006
Location: Hobbsville, North Carolina
Posts: 1,364
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Well, I pulled the outdrive and then the engine friday morning. after looking and comparing the couplings the old coupling wasn't worn as bad as I thought . The splines on the drive shaft looked like new. I found a couple of engine bellhousing bolts loose and the front mount adjustment nuts had worked loose too! After replacing the coupler I borrowed an alignment tool and realigned everything. It seems to have almost entirely eliminated the vibration. I havent taken it out for a good test but it ran pretty smooth on the hose. It took the better part of Friday but I think it will be worth the time and work!!
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77 V20 cuddy with 170 I/O Mercruiser
72 16ft. Carolina w/a 25hp Evinrude
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