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			#1  
			
			
			
			
			
		 
		
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			chum, you emailed this to me about 2 years ago. this is the adjustment for the cable that goes to the outdrive.  
		
		
		
		
		
		
			ferm, i adjusted the cable shown as much as it would go. the other cable is the problem. it still grinds a bit going into reverse. how do i adjust the cable from the controls to the bracket so i can get more of a positive shift into reverse? ![]() HHEEEEELLLLLPP ? ? ? ? ? ? 
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	hammer aint. stinkpot aint. sawdust aint. rainbow aint. maco sure as sh!t aint. randle? ha ha ha.  | 
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			#2  
			
			
			
			
			
		 
		
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			Have you tryed moving the bolt up in the slot to allow for more travel yet? If not I would do that and then readjust forward to get some more engagement.
		 
		
		
		
		
		
		
			
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	2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD ![]() AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664  | 
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			#3  
			
			
			
			
			
		 
		
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			yup. i moved it all the way up so theres no adjustment left.
		 
		
		
		
		
		
		
			
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	hammer aint. stinkpot aint. sawdust aint. rainbow aint. maco sure as sh!t aint. randle? ha ha ha.  | 
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			#4  
			
			
			
			
			
		 
		
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			If it hasn't allready been done, it may be  time to replace the shift shaft in the lower unit, its not a hard job, you will need one special tool, but there are ways around that. If it has the original shift shaft, it may have corroded enough to allow slop in the splines, casuing you to not have enough travel to  achieve proper shifting, there are several other reason for the shifting to be out, but this is a good place to start
		 
		
		
		
		
		
		
			
		
		
		
		
		
	
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			#5  
			
			
			
			
			
		 
		
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			I would start by removing the cable from the control, and then see how much play you have in the actual shifting mechenism. Then if you find quite a bit of slck, check to see if you can find out where it is at. It could be that the shift shaft bushing inside the bellhousing is just worn out and sloppy. You may still have the old style bushing in your current unit which won't take much wear.
		 
		
		
		
		
		
		
			
				__________________ 
		
		
		
		
		
	
	2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD ![]() AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664  | 
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			#6  
			
			
			
			
			
		 
		
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			Check the arm circled in red to see if it is loose on the shaft or if the roller in the end is broken. Then check to see if you have the large bushing like pictured circled in blue, or if you have a small bushing. Another area to check is where the yellow arrow is pointing. The cable could be loose and moving back and forth inside behind the allen screw. 
		
		
		
		
		
		
			 
		
				__________________ 
		
		
		
		
		
	
	2011 SUNDANCE B20CCR SKIFF, 2011 YAMAHA 90HP 4 STROKE, 2011 KARAVAN SINGLE AXLE ALUMINUM TRAILER, LOWRANCE ELITE-7 HDI, MINN KOTA RIPTIDE TROLLING MOTOR 2000CC HYDRA-SPORT 225+HP EVINRUDE SOLD ![]() AND THE PINK JEEP!!!! R.I.P. http://www.wellcraftv20.com/communit...ad.php?t=11664  | 
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